Well I thought I should try keep this updated, so recently things have started getting better :nod: yesterday I took the car to redditch for the remap with Greg Gush at Protuner.
Where after a couple of small issues such as boost leaks and the exhaust vband leaking were fixed, it finally made it on the dyno :thumbs:
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First run didn't go to well only making 310bhp due to the cam timing that Horsham developments done so Greg redone the cam timing resulting in a impressive 414BHP
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After speaking to Greg, he said the setup was capable of so much more but having a stock bottom end we could'nt really push it any more..
It made 375 torque, again we was going to push for more torque but means more boost. At the moment the boost controller is set to external wastegate pressure only.
The noise of the car now is absolutely epic
that really is the only way to describe it.. I've spent the day today sorting all the little bits and pieces and hopefully get to drive it tomorrow.
I know you are thinking, what you haven't driven it! I refitted the fan crowling and its catching on the fan now so can't drive it until its sorted.