Time for an update.
Since i put the brakes on a couple of months back i have covered around 1000 miles on them and they feel pretty good! Still haven't really driven hard with them yet but they feel so much nicer than the standard setup. I also fitted a BMC at the same time so not really sure if this improved the braking or not, hoping to book a track day somewhen soon so will find out then!
Ive had a knocking on the front end for ages and found that one of my tie rod ends had some play in. Replaced them with Some Tein tie rods and ends, along with new boots and front and rear drop links.
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This did firm up the front end nicely but annoyingly there is still a loud knocking coming from the front end of the car. After putting it up on a ramp we found the steering rack has play in it and the steering rack bushes are knackered! Ive ordered a rack from an S14 this evening and some super pro bushes from drift works so hopefully this will solve the problem!
Since the turbo arrived a few months back i have collected a few more parts to push the bhp up, took a few days off work this week to fit all the goodies below!
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Started by fitting the Nismo 740's, wasn't to hard as the ones i bought were already in a rail
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Put it all back together and it started up and ran perfectly so got to work on removing the buggered turbo!
This is my massive workshop by the way haha, but at least its dry so i won't complain
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Took me quite a long time to get the turbo and manifold out as I've never really done anything as big as this before, plus there was one b*****d of a bolt holding the turbo to the elbow which took me about 2 hours to undo! (Partly because it was soooo tight and partly because somebody has stolen my 13mm ratchet spanner).
Got it all out in the end though!
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After removing the turbo i found that 2 out of the four studs holding the manifold to the turbo were loose and one wasn't even there anymore :|, must have just vibrated out over time i guess! There was only about half of the gasket left in there too so don't know how i didn't hear it blowing!
Felt the shaft in the old turbo and there was quite a bit of play which i knew already, plus one of the water lines had been leaking for ages so was good to get all the old stuff off.
New and Old
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Fitted the new DW lines and put the turbo and manifold back together. Used new studs and nuts and all new Nissan turbo gaskets, also used loctite on everything so hopefully won't have the problem of it coming loose again.
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The turbo went back in and the car started up fine again with no leaks or warning lights
The Had somebody make up a recirc fitting for the Hks Bov because I'm too tight to pay £30 for one online!
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Fitted the new cold intake pipe from Apex performance to replace the stock rubber one, also to fit onto the New Z32 AFM. I bought a Tomei plug to make wiring in the New Maf easier but didn't realise the wiring diagram would all be in japanese.... So with a few dodgy online pictures and a bit of guesswork i managed to wire it up myself. Haven't had any warning lights and the car runs fine so must have done it right!
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Also did a full service on the car with oil, filters, plugs and coolant so now she's just waiting to be mapped!
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Took the front bumper off this evening to get it on the trailer and this is how the car currently sits, with my alarm set for 5.00 am for the trip up to Protuner
. Will see what she makes tomorrow!
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